Posted 07 June 2008 - 08:30 PM
Another update, me and vdubben today replaced my whole aum engine loom for s3 APY loom and I am going for complete S3 APY management. The advantages of this are that I dont now have to go for a custom AUM map but also the AUm ecu's are prone to throw up more fault codes and to put it plainly the s3 management doesnt actually give a foobar, lol.
Spoke to BNB today and he has all the bits I need to get the car up and running; injectors, 3" maf, APY ecu and hitachi coilpacks. So im going to pick those bits up tomorrow and trade some my remapped ECU and other bits and get this beast running!
Got some pics il upload them when I get back to a pc with a dongle!
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Posted: 09 June 2008 - 02:07 PM
right got the pictures, got the 3" maf, and 3 ecu's to try out, unfortunatly one of the ECU's was a BAM one and the other 2 were for AMK S3's (which are pre 2000). The problem with this is that my keys and clocks are 2001 and therefore we cannot add the Ecu so it'l run. We temporarily used an ARZ ECU to get the car started and running. Just need to pick up the hitachi coilpacks, APY ECU and 210 injectors and then she'l be driveable! Below are the pics:
S3 loom:

AUM loom out:

S3 loom going in:

Had to modify the wiring for the throttle body as the s3 ones are on the right hand side and the mk4 ones are on the left:

s3 ECU's and 3" maf:

The car running - I wish the sound quality is better, the flutter goes on for about twice as long as it did with the KO3s, the decat sounds brilliant too!
Golf with the Ko4 running - click hereGoing to pick up the rest of the bits today. We did a full vagcom on the car and there are no fault codes, it just doesnt deliver the power properly due to the injectors being the 150 models

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Posted: 24 June 2008 - 11:46 AM' timestamp='1214304361' post='1370020']
Right a little update for you all. I had a problem with the car cutting out once we had it running properly, this was because the selector in wrong and everytime I thought I was selecting 1st I was actually selecting 3rd. So we sorted that out on friday just gone and changed my suspension over for a set of FK coilovers taken from my mates donor car which you'l see in the pics later. Had a bit of a manic day on saturday trying to get the car ready for inters. After getting it running and taking it out for a spin, I noticed that I had a bit of a problem with my left wheel and suspected my wishbone might be a bit tired as this has never been changed in the whole 4 years I have owned the car so I set about doing that while everybody else was doing their prep work for the show, vdubben sprayed his car and everybody else just did last minute bits:

Off came the wishbone:


As you can see the rubber is pretty buggered on the wishbone as I thought!

So I went to our donor mk4 and took the wishbone off that - sweet!

Went back and started to fit it - this is the first one I have done by myself may I add B)


Back on and all sorted now I had to go about replacing some oil breather pipes on the car:

Sorted it then went for a drive and the system was airlocked as you can see by the puddle of water coming out from underneath my car and got an overheating problem because of this and because my thermostat was broken

So we took it out and I got another one at International on sunday for �12 a 70 degree one too so it'l run cooler which is better for me as I got a big front mount blocking my rad and taking allt he air - lol!

We then went to wash the cars for inters at 11pm at night - lol!

Went for a big drive that night to make sure the car was fine, ignoring the tempreture fluctuations it drove brilliantly. Got up early for inters (4am) and went to the petrol station with a few of the boys to fill up:

She was hot and had lost alot of water so I bought some anti freeze and filled her up, stupid me as this put another air lock in the system, drove it for about fiften minutes and then had to leave her at a petrol station as she wouldnt have made the journey and didnt want to make everybody wait for me.
When I came back from inters I got her home changed the thermostat and got rid of the air lock and she is perfect again! So anybody at Brands hatch tomorrow come and say hi!