The main reason I didnt remap this car on the day was the way the bost was acting, if it was a quick 300-400mb over shoot spike at 2700rpm then I would have been happy to tune it as I would say 99% of all 150PD will have this overboost stock or tuned.
My major gripe was that the boost held 400-500mb over boost close around -800-1000rpm the took a dive to 300mb underboost, tuning the car would have resulted it the boost going way over 1.9bar, even upto 2.2bar.
The VNT arm and actuator moved nice and free, both me and Jim checked it twice by and and mini vac pump, plus the actuator diaphragm reaction time was spot on, but this dont mean the actuator is 100%.
To sort this car out a lot of logging and trial and error testing is needed, start with the basics clean the erg and inlet manifol at the same time replace all the old vac lines. If still over boosting change the N75 valve, if that dont cure it then change the actuator.
I can and will be a pain to diagnose.
Nick