The car spent the day in the capable hands of Nick at carbon to try & find my missing power. When first mapped it made 205bhp & 245ft/lbs however at the RR day earlier in the month it only managed 187bhp & 200ft/lbs

The maf was replaced with a new Bosch one which didn't resolve the problem. Today Nick sorted out some dodgy pipework, fixed a very slight boost leak and did lots of logging.
The result was 194bhp & 200ft/lbs which is slightly better & the car is running better but its still down on torque massively

The logging showed a peak of only 11psi, however it confirmed that both the n75 & MAF are working correctly. The n75 is requesting the correct amount of boost & its just not being delivered. This means the problem is likely to lie with the actuator
