22 Sep 06
Good News or Bad news 1st?
Bad 1st. On my way to work yesterday this happened!

I was already suspicious of that hose but it seemed to be OK till now. It burst just by Middlesbrough Football Stadium so i had to walk into middlesbrough and get the bus home. Can you believe how much the bus costs now a days! The same journey used to cost me 50p when i was young and its not £3.30! Anyway i nicked the wifes car and went to the breakers yard where i knew there was a valver. He let me have the hose for £1 which i though was a bargain! It turned out that it was a little shorter than the original so a bit of copper pipe was needed. Thankfully i had come prepared and brought some with me! So a new hose and some new pink coolant later all was fixed. Only cost about £7 in total.

Oh by the way its the coolant hose that comes off the side of the head and goes to the heater matrix.
Because i needed to get it fixed i took the day off work, i don't know how thats going to work cos i don't have any holidays left! Hopefully they will just forget about it. So with the rest of the day free i decided to get some more jobs done and had quite a productive day. 1st i checked that i had the correct adaptors on each wheel as i though i may have put 30s on the front instead of 25's, but it turns out all of them are 30's, so thats OK then.
I then got side tracked a little when i found a bit of usefull looking hose that fell off the wifes rover. It was the cold air feed but its mine now! Ha ha! I cut a bit off the airbox and secured the hose in place like so.


And at the front i used another bit of hose thingy i had in my bits box to create the intake.

I thought it was a bit flimsy and looked a bit scew if so used some more plastic hosing i had to create an insert. So it all now looks like so.

With that done i can now re attach the side part of the airbox to quieten down things a bit. Ive kinda gone off the whole induction roar noise. Just makes me feel like a chav.
Next up i decided to have another bash at setting the ignition timing. At 1st i didn't really have a clue what to do, i didn't understand all this 6 degrees nonsense. After asking a few questions i realized that 6 degrees was the big notch cut into the flywheel. So i found some white touch up paint in my bits draw and marked up the flywheel groove for another go. I ran the engine at idle with the ecu vacuum pipe disconnected then shone the timing light into the hole. No matter where i rotated the dizzy the marks where no where to be seen. The bolts for the dizzy can go in 1 of 2 holes to allow for more rotation in either direction so i moved the bolts into the other 2 holes. This allowed me to rotate the dizzy some more. So i shone the light in again and rotated some more. Then voila! the marks appeared and lined up! As soon as the marks lined up the engine started to idle much higher so i adjusted the idle screw to match. Now the engine revs soo much free'er and has allot more power. The timing must have been a mile out! So I'm dead chuffed now, cant wait till tomorrow to get it RR tuned!
Now that i was on a roll i started looking for the cause of the squeal. Burnt fingers n ear later i found it to be the gasket between the lower and upper intake manifold. So i happy with that, it will just need splitting and re sealing with some silicone. Gonna do this tonight.
I also plumbed up all my LPG system which I'm going to test this lunch time so that the tuners can set up the LPG properly for me.
Even though i hurt my back doing all of this I'm much happier with the car now and a smile is returning back to my face.ÂÂÂ
